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Conference Papers | 2005 Victorian Conference Papers
FILTER
OPTIMISATION AT VICTORIA'S LARGEST WATER TREATMENT PLANT
Mark
Jarvis, Process
Engineer,
Melbourne Water Corporation
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ABSTRACT
The
Winneke Water Treatment Plant was subjected to an extensive
filter optimisation programme. Pragmatic applications
were used that can be readily applied to any conventional
filtration plant. This paper disseminates robust and
practical solutions assisting other engineers and operators
better utilise their filtration plant.
KEYWORDS
Conventional
rapid sand filter, optimise, backwash sequence, control.
1.0 INTRODUCTION
Melbourne Water's Winneke Water Treatment Plant has
a capacity of 450 ML/d and supplies up to 30% of Melbourne's
drinking water.
It was commissioned in 1980 and is located north east
of Melbourne, adjacent to Sugarloaf Reservoir. The reservoir
is an off line storage where water is pumped from the
Yarra River and Maroondah Aqueduct.
Sugarloaf
Reservoir water is pumped to Winneke's inlet structure,
where it is dosed with lime and alum. A flocculant is
used to aid clarification in 4 upflow solids contact
chambers. Clarifier supernatant is filtered through
12 conventional rapid sand filters. Filtrate is chlorinated
and pH corrected with lime prior to entering the clear
water storage. Treated water is distributed to the water
supply system on a demand basis.
2.0
WHY WAS FILTER OPTIMISATION REQUIRED?
In recent times the Winneke Water Treatment Plant has
regularly operated at flows greater than original intended
capacity. Efficient filtration and backwashing became
essential, however filters were operating significantly
below optimal performance.
A further driver for efficient filter operation was
the current project of increasing Winneke's capacity
to 620 ML/d. New filter design and operation is based
on existing filters. Successful commissioning relies
on established filters having an effective backwash
sequence. A consultant also carried out an audit identifying
a number of possible process improvements.
The
Winneke filters required a multi-pronged strategy of
reform. One prong incorporated improvements to an inefficient
backwash sequence. The second addressed media height
differences on either side of the filter gullet. The
third was to reduce media losses. The fourth was flow
hunting. The final prong identified and rectified a
number of other process improvements.
As filtration involves a myriad of operating variables,
optimisation was a compromise between conflicting target
parameters.
3.0
STEP BACK TO THE ORIGINAL DESIGN
Treatment plant operating parameters regularly change
to accommodate for current climate, raw water quality
and plant upgrades. As time marches on, these parameters
can deviate significantly from the original design.
Current operating parameters should be periodically
scrutinised against the plants' original design.
3.1
Backwash Sequence
The Winneke filter backwash sequence had strayed significantly
from the original design. The sequence that was used
is outlined in Table 1.
Table 1: Previous Backwash
Sequence

Note:
The sequence detailed above is similar to most of the
12 Winneke filters.
This backwash sequence included a number of steps that
provided minimal additional value. Backwash water flowrates
were not sufficient for adequate media expansion. Air
scour rates were below limits recommended for adequate
flocculant break up. Each filter backwash sequence was
different, resulting in unequal performance. This inefficient
backwash sequence began during a 1997 PLC upgrade. Following
any control upgrade, the original design should be reviewed
ensuring a reliable transition between systems.
In
an attempt to increase backwash efficiency, in February
2005 the sequence was changed to closely follow the
original design manual:
Table 2: Original Design Manual
Backwash Sequence

Note:
These air and water flowrates are at near maximum available
capacity.
Reverting
back to the original design resulted in significant
reductions in backwashing time, backwashing volumes,
energy consumption, operating costs and headloss.
3.2 Filtered Water Flow Control
Original
plant design intended filtered water flow to be controlled
from the level in both the clarifier inlet and clarifier
outlet. However, for many years only the clarifier outlet
level was programmed to control. This resulted in a
rapid control loop causing filtrate flow hunting of
80 - 100 ML/d every hour. This caused a number of process
difficulties, most notably chemical dosing control.
A
trial began on July 4th 2005 with filtrate flow controlling
according to original design. As shown in Figure 1,
flow variability reduced.

Figure 1: Filtrate Flow Before
and After Control Change
Further reductions in flow variability were subsequently
achieved through control tuning. Reduced backwash water
volumes also facilitated reduced flow variation.
Flow spikes in Figure 1 indicate backwashing. As backwash
water is supplied from the filtered water channel, flow
variation during backwashing is unavoidable without
significant capital upgrade.
Using
all available July 2005 data, flow and pH variability
prior to and following the control change is outline
in Table 3.
Table
3: Flow & pH Variability Prior to and Following Control
Change

Reverting to the original plant design reduced flow
variance by 18%, and more importantly reduced pH variance
by 49%.
4.0
BEYOND ORIGINAL DESIGN
Operating a plant based on the original design is not
likely to achieve optimisation. The plant engineer or
operator must also consider other steps to attain this.
In the years following design, the goal posts of what
is perceived as best practice will shift. Operating
parameters must be periodically reviewed to ensure contemporary
treatment practice is adopted. Optimisation is a perpetually
moving target.
Invaluable insight can be gained through communication
with a plants' original design engineer. Auditing consultants
can identify possible process improvements. Detailed
searches on recent literature such as AWWA's 'Water
Quality and Treatment, 1999' and Kawamura's 'Integrated
Design of Water Treatment Facilities, 2000' will
also assist optimisation.
4.1
Communicate with Original Design Engineer
Discussions
with an original Winneke design engineer concluded 'filter
under-drains and launders were not originally designed
to operate with a combined air and low flow water step'.
The Winneke WTP was commissioned at a time when current
industry thinking adopted the combined air and water
step, even though the plant was not designed for this.
Winneke WTP has always operated with this combined air
and water backwash step, as specified in the original
design manual.
Further
trials were undertaken with the combined air and low
flow water step removed. This two-step process of air
only, followed by high rate water yielded reduced backwash
time, backwash water volumes and operating costs without
compromising backwash effectiveness.
The
original design engineer can provide insight of the
intended functionality and process design philosophy
of the plant.
4.2
External Process Audit
A water treatment consultant, City Water Technology
carried out a preliminary process audit at Winneke in
November 2004. This identified a number of possible
process improvements. Many of these recommendations
facilitated improved filter operation.
4.3
Backwash Water Optimisation
After
reverting the backwash sequence back to the original
design and removing the combined air and water step,
the backwash sequence included air scouring followed
by high rate water washing.
Backwash water turbidity at termination of backwashing
should be 10 - 15 NTU (AWWA, 1999). This provides optimal
filter media cleaning and minimised wash water volumes.
Grab samples were taken during backwashing to determine
when this occurred. Depending on process conditions,
this was typically after 5 minutes 20 seconds.
The
final optimised backwash sequence is detailed in Table
4. This sequence varies greatly from the previous sequence
(Table 1) and the original design (Table 2). This technique
is an extremely powerful filter optimisation tool. It
should be repeated regularly to maintain optimisation.
Table 4: Optimised Backwash
Sequence

The new backwash sequence does more with less. It resulted
in:
-
38% reduction in backwash water volumes, or over 700
ML per annum.
- Operating
cost reduction of ~$30,000 pa due to reduced water
treatment and energy costs.
- Backwash
pump and blower extended life due to reduced operation
time.
- Increased
filtration capacity of 3.5 ML/d due to:
- Backwash
water volume savings (2 ML/d)
- Backwash
time savings provided increased production time (1.5
ML/d).
Optimising backwash water flows and times by measuring
backwash water turbidity can provide significant operational
savings.
4.4 Backwash Draw Down Level
Current
industry thinking deviates from Winneke's original design.
Prior to commencement of backwashing, filters have always
drained to significantly below the top of the media,
as specified in the original design. Current industry
practice suggests levels should be 25 - 50 mm above
the media surface to improve flocculant break up. Level
probes were subsequently elevated to achieve this.
4.5
Reject To Waste
A filter ripening trial occurred where reject to waste
(RTW) times were adjusted to determine the effect on
filtrate water quality. During each filter ripening
period, turbidity typically increased from 0.05 NTU
to 0.07 NTU for approximately 10 minutes. Particle counts
typically increase by approximately 600% above normal
filtrate levels for approximately 5 minutes.
It was found there is no correlation between the RTW
time and filter ripening data for RTW times up to 20
minutes. RTW times over 20 minutes are not operationally
feasible. A filter with no RTW can have superior water
quality than a filter with a long RTW.
Although
inclusion of the RTW is generally recommended to control
protozoan organisms, it did not improve filtrate water
quality. Its removal increased filtration capacity by
220 ML pa, reduced operating costs by $3,000 pa and
improved plant reliability.
The original design RTW time was 3 minutes and the old
backwash sequence RTW was 1 minute. However, optimisation
was achieved with no RTW. Once again, contemporary treatment
practice deviates from the original design.
5.0
FILTER MEDIA BED HEIGHTS
Media heights were not the same on each side of a filter
gullet. This is predominantly due to low gullet launders,
a history of inappropriate backwashing and air entrapment.
Height differences ranged from zero to 300mm. Height
differential resulted in different hydraulic capacity
on each side of the gullet. This caused poorer filtration
on the low media side.
Filter
media levels on each side of the gullet must be equal
to achieve optimisation. A differential height impacts
filtrate turbidity, media sludge concentration and sand
carryover.
5.1 Equalising Media Heights
Media heights were equalised using a crane and excavator
to transfer a calculated volume of sand.
5.2
Effect on Turbidity
Filters with greater media height differential on each
side of the gullet had increased filtered water turbidity.
This relationship is shown in Figure 3.

<Notes:
This correlation is an original finding; all datasets
yield similar results to above; each data point represents
one filter.
Figure
3: Filter Outlet Turbidity vs Media Height Differential
on Each Side of Filter Gullet
Following levelling media heights, equal filtration
occurred throughout the bed. This facilitated reduced
average filtrate turbidity from 0.060 NTU to 0.052 NTU
(13%). This
mitigates public health impacts by facilitating reduced
protozoan risk.
5.3
Effect on Media Sludge Concentration
Media
grab samples were taken and sludge volumetric percentage
measured. Media sludge concentration was found to be
a function of media height. The greater the media height,
the greater the media sludge concentration. Following
media height equalisation, sludge concentrations became
similar on each side of the gullet.
5.4
Effect on Sand Carry Over
Filters
with a greater media height differential between each
side of the gullet were found to have greater overall
media loss.
The filter with the greatest media height difference
(300mm) lost the greatest volume of sand (over 30%).
This is due to a lower pressure differential across
the low bed, causing greater backwash flows. This creates
additional turbulence in the low bed, which promotes
sand carryover. Media height difference and media loss
is a snowballing problem.
6.0
AIR ENTRAPMENT, SAND CARRYOVER AND SAND LOSSES
Sand
has carried over into the Winneke filter gullets since
commissioning. From 1980 to 2005, each filter lost an
average 0.28m of the original 1.00m of sand. An investigation
into the cause of this sand carry over was undertaken.
During backwashing, a very significant amount of air
rose through the media bed for up to 8 minutes after
the air blower turned off. This gave the appearance
of air scouring in a section each filter. The rogue
air rose whilst high rate water flowed over the launders
and into the gullet. This contributed significantly
to sand carry over.
Further investigation found the backwash water system
normally contains approximately 40 m3 of air. This was
the source of the rogue air.
Backwash water pump non-return valve sealing tests found
profuse leaking. This allowed water to pass from the
backwash water duct into the backwash water tank. Large
volumes of air then entered the backwash water duct
through an air valve. After replacing all backwash water
pump non-return valves, the majority of air escaping
through the bed ceased. Leaking valves were a major
cause of trapped air and sand carry over.
Sand carry over was also attributed to a history of
inadequate backwashing and low filter gullet launders.
Excessive backwash water system air ingress must be
absolutely avoided to minimise sand carry over and sand
losses.
7.0 PEA GRAVEL LAYER
Winneke
WTP originally had a 150mm pea gravel layer below 1000mm
of sand. Pea gravel is now scattered throughout the
sand. In some sections the layer no longer exists whilst
in some sections the gravel layer is over 500mm. This
significant pea gravel disruption is due to the backwash
water control valve operation speed, a history of inappropriate
backwashing and air entrapment.
7.1
Backwash Water Control Valve Operating Speed
'Opening the backwash valve slowly is essential(to
prevent) gross disturbance of the gravel' (AWWA,
1999). To reduce disturbance of what is remaining of
the pea gravel layer, the backwash water control valve
opening time was increased from 9 seconds to over 60
seconds. Similarly, the backwash water control valve
closing time was increased from 9 seconds to 30 seconds
to help reconstruct the pea gravel layer.
7.2
Backwash Sequence
'Movement of the gravel can also occur when air scour
and water backwash are used simultaneously' (AWWA,
1999). This occurred for extensive periods during the
old backwash sequence. The optimised backwash sequence
has no combined step. It also has a long high rate wash
step to aid bed reconstruction.
7.3 Air Entrapment
Trapped
air released through the bed during the high rate water
wash contributed to pea gravel disruption. Backwash
pump non-return valve replacement has reduced trapped
air. This will reduce pea gravel disruption.
8.0 HEADLOSS
Optimised
filtration provided the following headloss reductions:
Table 5: Average Headloss Prior
to and Following Optimisation

Note:
May 2005 data was used.
Optimised
filters have reduced headloss, which facilitates filter
run times of over one hour longer.
9.0
CONCLUSIONS
Significant operational gains can be made from vigorous
water treatment plant optimisation. This process should
occur periodically and involve trialling original design
specification operating conditions, reviewing and adopting
current industry literature, engaging a water treatment
process auditor and if possible communicating with the
original design engineer.
Winneke
Water Treatment Plant filter optimisation reduced annual
operating costs by $30,000, reduced filtrate turbidity
by 13%, increased filtration capacity of over 4 ML/d,
reduced media losses, reduced headloss by 15%, reduced
flow variance by 18%, reduced pH variance by 49% and
reduced annual backwash water requirements by over 700
ML.
10.0
ACKNOWLDEGEMENTS
The
unequivocal solidarity from all Winneke WTP personnel
(Glenn Collins, Graham Sangster, Jim Phillips, Cyril
Barber, Brian McNeil, Keith Craine, Barry Hastie, Pieter
Mollema, John Devries, Gerald Fitzgibbon) has ensured
the project yielded a number of positive outcomes.
Wayne
Waters (United KG) and Bruce Murray (City Water Technology)
provided valuable water treatment process operation
expertise.
11.0 REFERENCES
American
Water Works Association Water Quality and Treatment,
A Handbook of Community Water Supplies 4th Ed (1999),
McGraw Hill Inc., New York.
Kawamura S. Integrated Design of Water Treatment
Facilities, 2nd Ed (2000), John Wiley & Sons Inc.,
New York.
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