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Conference Papers | 2003 Conference Papers
FILTRATION
BACK ON TRACK
Michael Bonanno, Production
Officer, Sydney Water
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ABSTRACT
Quakers
Hill Sewage Treatment Plant (STP) is Sydney Water's
second largest inland STP, discharging an average of
32 megalitres per day of tertiary treated effluent into
Breakfast Creek. The EPA regulates the effluent quality
in order to protect the aquatic environment of the Hawkesbury/Nepean
River System. Work has recently been completed to improve
the reliability of four Travelling Bridge Filters, resulting
in improvements in treatment performance and saving
millions of dollars in deferred capital.
Filtration
is an important process for the removal of phosphorous,
suspended solids and faecal coliforms from wastewater.
Quakers Hill STP's licence requires all flows up to
900L/s to be filtered. The aim is to produce an effluent
with an average total phosphorous of 0.05mg/L (year
to date performance is 0.03mg/L). Four dual media filters
and four travelling bridge filters (TBF) comprise the
filtration process. For over ten years the TBF have
been very unreliable. The dual media filters alone are
capable of producing high quality effluent during dry
weather, however quality has traditionally been compromised
during wet weather.
In
1989 four TBF's were built to supplement the four dual
media filters. A TBF is a down-flow, single media, shallow
bed filter that is broken up into many individual cells.
The main advantage of the travelling bridge filter over
a dual media filter is that filtration capacity is maintained
during backwashing while still producing an effluent
quality adequate for wastewater applications. The backwash
system is mounted on a bridge, which travels slowly
along the filter, backwashing each cell individually.
The filter backwash operates by pumping filtered water
through the sand bed into each individual cell. A wastewater
pump takes the dirty backwash water out of the filter
into a waste channel.
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Since
commissioning, the TBF's were plagued with problems.
Two major problems were bridge derailment (pictured
Left) and sand migration (pictured below).
Bridge failure can lead to a series of other problems
such as damage to limit switches, rails, wheels
and bearings.
The
filters would need to be taken offline for extended
periods to be repaired. The sand migration problem
would occur as a result of numerous backwashes;
always some sand would be dragged to one end.
The sand at the end would prevent the bridge from
reaching its limit switches and so cause damage
to wheels and rails, as well as derailment. The
two major problems were very much inter-related.
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years of reacting to near daily problems two options
were considered. One was to demolish the TBF's and
install four additional dual media filters, which
would incur a high capital cost. The second option
was to take a less expensive, in-house approach
to discovering and addressing the root cause to
these problems and establish reliability of the
TBF's. The in-house optimisation approach was given
priority over the rebuild approach. A small team
of planning staff, production officers and maintenance
workers were introduced to the TBF problems in December
2000. A brainstorming session was conducted to identify
all possible causes for the inherent problems. It
was believed that derailment could be avoided by
investigating the alignment of the bridges and axles.
A
maintenance crew was assigned to check and adjust
the alignment of the drive system.
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After
the bridges were realigned, they ran for several weeks
without misalignment. However, problems with sand build-up
were still causing the wheels to climb the rails on
some of the bridges. This was not observed at other
TBF installations. The wheel shape was compared to other
Sydney Water STP installations and the cross sectional
shape of the wheels was found to be different. It was
believed that an H-shaped wheel would completely eliminate
any derailing.
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new wheel was manufactured and installed and the
alignment was checked and rechecked. (The old
wheel is the left picture; the new H-cross section
is the right picture). This work was completed
by June 2001. This work was successful since no
further derailments have occurred. The elimination
of the derailment problem was an important milestone
for this project because it allowed for operational
issues to be addressed without the threat of derailing. |
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The
filters were now able to run for weeks without stopping.
The only problem was that after a few weeks, sand
would build up on the ends and prevent the bridge
from reaching the limit switches, causing damage
to the wheels and rails (pictured Left).
It was unknown how this would be solved so the first
thing was to check if the filter was operating according
to the design. The waste water and backwash pumping
capacity was designed to be 11L/s. The original
pump size was 11L/s and the actual pumping rate
was found to be 3.5L/s. It is believed that head
losses in the system were incorrectly calculated
resulting in undersized pumps. |
A filter was selected to trial a pump designed to pump
30L/s. Modifications to the filter were required to
accommodate the larger pumps. After installation the
pump flowrate was found to be a maximum of 13L/s, which
can be turned down by the operator. The problem with
sand migration was reduced when compared to the filter
with the undersized pumps. As a result, all the backwash
and wastewater pumps were replaced. This work was completed
in March 2002.

Overall
the work has been successful in improving filter reliability.
As a result of TBF reliability improvements Quakers
Hill STP is able to reliably achieve high quality effluent
under all weather conditions. Full credit goes to the
Production Officers at Quakers Hill STP for their operational
support and problem solving skills, Sydney Water's Planning
Team for providing technical support and finances and
our maintenance staff for solving problems with wheels
and alignment, and, for making the modifications required
to install the new pumps.
As
a result of this cooperation and determination, filtration
at Quakers Hill STP is now BACK ON TRACK! DOWNLOAD
(pdf
587KB)
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