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Conference Papers | 2003 Conference Papers
POLYMER
MANAGEMENT AND TREATMENT ALARM USING THE IQ SENSOR SYSTEM
ULTRASONIC TURBIDITY PROBE
Alex
Dupleix, Treatment
Plant Manager,
Warrnambool Cheese & Butter Factory Company
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ABSTRACT
The
Warrnambool Cheese and Butter Factory wastewater treatment
plant incorporates an induced air floatation system
to remove suspended solids from the Anaerobic treated
effluent. Failures in the floatation cell could lead
to high levels of suspended solids being discharged,
causing a negative impact on the operation of the South
West Water Authority wastewater treatment plant at Thunder
Point.
An
alarm system needed to be in place to prevent discharge
of high solids.
Turbidity
was chosen as the alarm trigger because the clear background
matrix could be detected by this method and ensures
effective treatment occurs. Several systems were trialed
unsuccessfully as the residual solids formed a scum
on the detectors and on the surface of liquid cells.
The
IQ Sensor Net system with an ultrasonic self cleaning
turbidity probe, has recently been installed at the
plant and has provided the answer to our problems. In
fact, the trial was so successful we handed over the
purchase order and said find another demonstration unit!
The
operation of the probe has been very successful. The
side of the probe builds up deposits but the 'measuring
window" has stayed clean. The IQ Sensor Net system
also has the advantage of connecting to our Citect automation
control system.
The next aim is to use the turbidity probe to fine tune
the chemical dose rates, thus optimising chemical use.
The IQ Sensor Net system was also chosen for its simple
expansion capability and its ability to control extra
probes. An ammonia probe and a pH probe will be added
in the near future.
The ph and ammonia levels are very important factors
in the operation of the anaerobic Bulk Volume Fermenter
and need to be monitored constantly.
1.0
INTRODUCTION
Warrnambool
Cheese and Butter Factory is situated at the end of
the Great Ocean road, 12 km east of Warrnambool. The
plant is 15 km north of Childers cove and the bay of
islands, two local features of the ship wrecked coast.
The company at peak season processes three million litres
of milk per day sourced from 600 farmers across south
west Victoria and south east South Australia. Warrnambool
Cheese and Butter factory's annual production is 34,000
tonnes of cheese, 24,000 tonnes of skim milk powder,
as well as butter, whey protein concentrate and packaged
milk etc.
The
Warrnambool Cheese and Butter Factory Waste Water Treatment
Plant originally consisted of an Equalization tank and
anaerobic Bulk Volume Fermenter (BVF) Reactor. The system
was designed by ADI, the Canadian company that perfected
this type of technology. The plant was built by KME.
The
function of the EQ tank is to equalize the pH and COD
loading and has a 6 hour retention time. A secondary
function allows for the separation of fat from the influent
stream.
The function of the BVF reactor is to provide anaerobic
treatment of the influent to reduce the COD load.
2.0
DESIGN CRITERIA
The
plant processes two to three times the design waste
load as shown in Table 1.
Table
1: Design criteria and current loadings

3.0
PLANT PERFORMANCE
The
plant is monitored daily by a NATA registered laboratory
to guarantee optimal performance. BOD reductions of
98.5% are achieved.
WCBF
have an after care agreement with ADI (ADI reviews operation
data and provides technical support plus site visits.)
The
plant was built in 1993. The original design included
anaerobic SBR but because of the prohibitive cost it
wasn't installed. The plant operated well at the design
loads, but as the influent loads increased the levels
of BOD and suspended solids in the treated effluent
rose to the point where they where having a negative
impact on South West Water's Warrnambool wastewater
treatment plant at Thunder Point
A
secondary treatment plant was required to meet the trade
waste standards set by South West Water for Warrnambool
Cheese and Butter Factory. Refer to Table 2 for loading
percentages prior to secondary treatment plant installation.
Table
2: Factory discharge as a percentage of South West Water's
intake load.

During
1997 an investigation was made into four alternative
treatment options:
1) A facultative lagoon
2) A lagoon style SBR
3) A chemically assisted clarifier
4) An air flotation cell
The following year the trade waste bill reached 1.5
million dollars and a decision was made to install an
air flotation cell. The air flotation cell was the preferred
process because it had the best capacity to remove the
suspended solids. The high suspended solids in the treated
effluent were having the greatest influence on the trade
waste charges.
4.0
THE JETFLOTE INDUCED AIR FLOTATION CELL (IAF)
The
Jetflote Induced Air Flotation cell was chosen because
of its proven ability in the dairy industry and simple
design.
The
heart of the Jetflote plant is the Jameson Flotation
cell which incorporates a vertical column of liquid
known as a down comer. The down comer pipe has a flow
rate 1.5 times the through put of the plant. A small
air bleed at the top of the down comer allows air bubbles
to be incorporated into the column of liquid. The bubbles
may be visualized as a stream of marbles moving down
the column. Polymer is also injected at the top of the
column, allowing the solids to flocculate and incorporate
the air bubbles. The flocculation process is completed
in the column. The base of the column discharges the
flocculated solids below the surface of the sludge separation
tank. The sludge is skimmed off to a holding lagoon,
while the clear treated effluent is discharged through
a third cell. Refer to Figure 1.
Figure
1: The Jameson flotation cell

The plant was commissioned in May 2000 and operates
continuously 24 hrs a day, 7 days per week.
The
foot print of the plant is small, allowing the plant
to be built off site and delivered skid based on a regular
transport. However, the plant has a short residence
time which means a failure can rapidly result in poor
quality effluent. For example, a failure with the polymer
dosing system could lead to high levels of BOD and suspended
solids in the treated effluent. This would result in
an increased trade waste bill, and may have a negative
impact on the South West Water treatment plant operation.
Table
3 sets out the hypothetical charges based on actual
data from the 2000-2001 year.
Table
3: Hypothetical trade waste charges

Based
on the average figures, poor performance by the IAF
has the potential to cost $11,000 per day.
[($4,500,000- $309,000)/365days =$11,000]
Potential
peak season costs could be close to $20,000 per day.
5.0
ALARM SYSTEM
An
alarm system is needed to alert the operator to poor
quality effluent, enabling the plant to be shut down
for repair. Turbidity was chosen as the alarm trigger,
because the clarity of the back ground matrix could
be detected by this principle.
5.1
Turbidity
The
principle behind the decision to choose turbidity was
that the clarity of the back ground matrix is proportional
to the suspended solids in the treated effluent. The
relationship provides a decrease in transparency of
the liquid due to an increase in the presence of undissolved
solids.
Turbidity
is measured by producing a light beam from a tungsten
lamp source. The beam of light is directed into the
sample. A detector is then used to measure the intensity
of the beam. The detector can be placed to read either
the reflected or backscattered light, the transmitted
light which has passed through the source, or light
which has been deflected at a specific angle. See Figure
2.
Figure
2: Light scattering and turbidity measurement
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1)
Back scattering of light
2)
Intensity of light passing unchanged through the
samples
3)
Intensity of scattered light in a special angle
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5.2
Selection of the First Turbidity Meter
The original instrument utilized two sources and detectors,
with the light beam passing through the liquid stream.
The use of two sources and detectors enabled two simultaneous
measurements providing better accuracy.
The unit was chosen for its accuracy, but it failed
to cope with the application.
The
Problems encountered were;
1) The large carry over particles affected the reading.
To overcome the problem the treated effluent was piped
directly from the centrifugal recycle pump. The action
of the centrifugal pump provided a sample of uniform
particle size.
2)
Small particles were still attached to air. These particles
floated to the surface in the sample weir adhering to
each other eventually blocking the chamber and the delivery
tube.
5.3 Selection of the Second Turbidity Meter
The
second instrument worked on the 3rd principle (refer
to Diagram 3), in which the light beam from the source
is reflected or scattered from the sample surface at
an angle to the detector. The measuring mechanism is
housed in a light proof box to prevent stray light interfering
with the result. Design advantages, which led to the
instrument's selection were the large sample handling
tubes, the bubble eliminator and the small sample detection
surface which was assumed to be self cleaning. There
was also provision to add a flush system to clear the
sample chamber and detector surface of flocculated particles.
The second detector system worked initially but the
next day there were problems.
1)
The small particles collected in the piping and floated
out in the surface well affecting light scatter and
hence the result. A flush system was installed and a
daily cleaning regime set up
2)
Another problem was the temperature of the treated effluent,
(32 degrees Celsius). At this temperature the light
proof box filled with condensation that interfered with
the integrity of the light beam.
Although we persisted with this unit, its operation
was never consistent enough to be employed as a monitoring
system. The concept of the quality alarm had again failed
to convert to a working system.
We
needed a system that did not involve the transfer or
handling of a sample in any way at all.
The
obvious solution was to trial a probe style detection
system. We began by inserting a bottle in the discharge
cell of the IAF plant to act as a dummy probe. As we
expected the small particles with their attached air
bubbles adhered to the bottle coating it in a biological
slime. It appeared that we had no way of achieving our
alarm system.
5.4 The IQ Sensor Net System
with Ultrasonic Self Cleaning Turbidity Probe
The
answer came when reading an article in a water instrument
supply company journal. The detector unit was a self
cleaning probe using ultra sonic vibration to prevent
accumulation of slime and mineral deposits over the
detector lens. We contacted the company and arranged
a trial. The trail was successful, so we purchased the
installed the system.
The
unit operated well, only occasionally requiring a wipe
clean. After a few months of operation it was observed
that biosolids were beginning to hang onto the probe
surface, but the two sensor points stayed clean. The
scum eventually began to interfere with the readings.
A mineral layer had built up on the sides but the detector
surface retained a shiny surface after wiping with a
cloth. Figure 3 shows the deterioration in the readings
due to the scum build up.
Figure
3: Effect of scum build up on probe

The
problem was overcome by adding an air purge to remove
the build up. The air purge was controlled by the Citect.
The Citect allows the frequency and the duration of
the purge to be altered by the operator. The air purge
could be controlled by the IQ Sensor Net system but
I wanted to see it on the screen.
Figure
4: Probe cleaning using air purge

Figure
4 shows the spikes due to the air purge and also the
increase in the turbidity reading during the plant shut
down.
The
turbidity measurement is now at the stage where a reliable
reading is being generated and an alarm set point can
be put into the Citect. The turbidity probe has also
helped us fine tune the polymer dosing rate, reducing
the dose rate by several ppm. The adjustments are made
manually at this stage.
A
further trial was carried out where all the variables
were fixed for example the surfactant dosing rate and
the plant flow rate. The polymer dosing rate was then
varied. The turbidity and dosing pump speed was recorded
and the corresponding sample tested for suspended solids.
The relationship shown in Figure 5 indicates that both
over and under dosing can occur with a safe range showing
the optimal dosing rate to be 6ppm.
Figure
5: Polymer dosing rate versus turbidity & suspended
solids

Figure
5 shows that it is possible to automate the dosing rate
to obtain the lowest turbidity.
6.0 CONCLUSION
The
process of realizing the original concept of an alarm
system for the treated effluent quality has been a long
and expensive one. But three turbidity meters later
we have the alarm working. The next step is to automate
the dosing set point using the turbidity probe. This
should optimise polymer usage and save operating costs.
7.0 ACKNOWLEDGMENTS
- Chris
Conway - Environmental Group (Jetflote) - Technical
- Phil
Edwards - Merck - Technical
- Paul
Weir - WCBF - Electrical
- Brooke
Mellington - WCBF - Automation
- Maurice
King, Helen Dupleix - Proof reading
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