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Conference Papers | 2003 Conference Papers
DETECTING
ODOUR POTENTIAL AT AN INDUSTRIAL TREATMENT PLANT
John Day, Wastewater
Treatment Operator, Norske-Skog
Newsprint Mill
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ABSTRACT
In
1998 Norske Skog, then known as Australian Newsprint
Mills, started an extensive program to reduce odour
that was being generated from its effluent treatment
plant. Section 4 (iii) of the Pollution reduction Program
issued to (then) Australian Newsprint Mills Ltd on June
15th 1998 required the company to:
"Prepare
and submit a report to the EPA on preferred options
for introduction of in-line continuous monitoring that
identify the onset of conditions for anaerobic decay
within individual plant units. The report must identify
operational contingency plans when the onset of conditions
for anaerobic decay are detected by the monitors."
The
purpose of this report is to summarise the work done
to fulfil the EPA requirement.
At
the AWWOA conference in 1998, the first findings were
reported on the odour reduction program about to undertaken.
This paper highlights the success we achieved in implementing
this program as well as further steps that were taken
to identify odour potential.
1.0
BACKGROUND
Norske-Skog
(previously Australian Newsprint Mills) has been operating
since 1981. It is situated on the Hume Highway 13 km
north of Albury. The mill produces newsprint through
a mix of wood fibre from Pinus Radiata, and recycled
fibre from recycled newspaper and magazines. The treatment
plant processes on average 8 megalitres per day of effluent.
Treating pulp and paper effluent can be broken into
three easy components - settle, cool and treat. The
traditional way to treat this type of effluent is to
store it as long as is needed to lower the solids and
temperature then either use an anaerobic treatment process
(ie larger ponds), or as in our case an aerated biological
process. Both of these can lead to one thing - strong
odour. In 1998 the Mill along with its neighbours, and
the EPA, mapped out a plan to reduce odour.
The
purpose of this report is to summarise the work done
to fulfil the EPA requirement to reduce the odours so
that they could no longer be detected by neighboring
houses, and if detected they were detected, allow immediate
actions to be undertaken to reduce the odours. After
putting into place major changes to the treatment plant,
the challenge then was to find a reliable early detection
program. Odour could then be dealt with before it became
detectable by the neighbours.
2.0
PLANT CHANGES
The
main plant changes made to remove odour being generated
were two fold. The first was to reduce the retention
time within the plant and the other was to raise the
pH. Retention time reduction was carried out in two
parts of the plant - at the Primary Clarifier and at
the Equalisation Storage, or Cooling Ponds. To reduce
the retention time in the Primary Clarifier, flows were
diverted to one Clarifier, instead of splitting all
flow to two clarifiers. This reduced retention time
from 25 hrs average to 14 hours.
The
capacity of the underflow pumps was increased so the
thickened underflow could be removed at a larger volume
to the presses. This reduced the chance for sulphur
producing bacteria to populate in any anaerobic pockets.
To
reduce the retention time in the buffer storage section
of the plant, an unused aeration tank was converted
to an Aeration Feed Tank (AFT). Large earthen cooling
ponds with a retention time of around 50 hours had previously
been in place. After converting to the AFT, the average
retention time of 24 hours was achieved.
The
purpose of the AFT, as an equalisation basin, is to:
- Cool
the effluent to less than 40oC to ensure efficient
biological treatment.
- Buffer
flow surges through the plant to protect the biological
process.
- Buffer
spike loads of toxic or high organic material to protect
the biological process.
- Ensure
adequate mixing to prevent deposition of solids and
assist with pH control.
To
ensure adequate mixing in the AFT we added 10 aspirators
located in position to circulate the flow.
2.1
pH Control
The
next change was to maintain the pH in the AFT by adding
lime controlling the pH to between 7.5 and 8.2. As shown
in Fig 1, when raising the pH above 7.5, the chances
of H2S being produced are reduced by transforming the
H2S into HS- and S2-. These are both aqueous species
and do not smell, whereas when H2S is formed as a gas,
it has a very offensive characteristic odour (rotten
egg gas). This forms the basis for the focus on pH control
in controlling odour, as maintaining a pH above 7.5
significantly reduces the proportion of the sulfide
that can exist as H2S. There is approximately eight
times as much odour (H2S) generated at pH 7.0 compared
to pH 8.0 for a given dissolved sulfide level.
Figure 1: pH Effects on Percentages
of Gas Production

2.2
Control Measures
The
study we carried out in 1999 identified areas that could
be more closely monitored to control odour now the main
engineering work had been completed. Any of the following
could put us into an odour generating condition:
- Failure
of the floating aspirators in the AFT. Evidence
has shown that the sulfide level in the AFT significantly
increases if the aspirators are off for any extended
period of time (>4 hours). It is essential that
if this occurs, the pH of the effluent is monitored
closely to ensure it is within the appropriate range
(7.7 to 8.2) to minimise the generation of H2S.
- A
drop in AFT pH below 7.5. The majority of the
days when odour was "noticeable" on site
occurred when the pH in the AFT was lower than 7.5.
It is important to note, however, that the lower the
sulfide concentration, the less important pH becomes
in controlling odour generation.
- A
rise in the AFT operating level above 1.5 metres
shows the effect of AFT operating level or retention
on the dissolved sulfide concentration. There may
be occasions when it is necessary to raise the AFT
operating level higher than 1.5 metres, such as during
major maintenance periods within the process plants.
During these occasions, odour will be managed by close
control of the pH in the AFT. Note that the normal
operating level of the AFT will vary between 0.9 and
1.3 metres in order to buffer any large flow surges
from the process. This can be seen clearly in Figure
2. When AFT retention rose, so to did the sulphide
test results.
Figure
2: pH Effects on Percentages of Gas Production

- Sludge
build-up in the Primary Clarifier. A thick primary
clarifier underflow increases the sludge residence
time and the chance of sulfide generation. Note that
although the primary clarifier is not a significant
odour source, this situation requires monitoring to
prevent extremely high sulfide levels being carried
on to the AFT.
After
successfully running under these operational parameters
for two years, we experienced one major problem of high
temperature due to the reduced retention time of the
Primary and the Equalisation Basin (AFT).
This
problem became larger when Pulp production required
a raise in the operating temperature to reduce pitch
deposits caused in the paper making process. Influent
temperatures were to be raised from 50°C to an average
75°C. This gave us only two choices - either increase
retention time and use chemical addition to reduce odour,
or stick to our odour management plan and install cooling
towers pre the aeration tanks. The cooling towers were
an obvious and logical choice. This also then gave us
the opportunity of using temperature to control odour
by using the higher temperatures to kill, or slow down
any odour producing bacteria. This has worked extremely
well in the primary clarifier in reducing sulphides,
as indicated in Figure 3.
Figure
3: Effects of Temperature on Sulfide Production

3.0
ODOUR POTENTIAL
During
the process of identifying the odour producing sections
of the plant several test methods were used to identify
odour. These included:
- Dissolved
Sulfide testing using the HACH method #8131;
- Redox
Potential using an inline probe;
- Subjective
odour surveys using Mill Staff and Community members;
- Volatile
Fatty Acids;
- Dissolved
Sulfates.
From
trials on these methods it was agreed by all parties
that Dissolved sulfides was a reliable test that could
be carried out by operators on a daily basis. Test points
identified to give us early indication were:
- Primary
Overflow;
- Primary
Underflow;
- AFT
outlet.
A
calculation that could be trended to give an early detection
was then identified. Fortunately, Thistlethwayte, had
developed an empirical correlation that predicts the
equilibrium gas concentration of H2S above a liquid
of a given sulfide concentration, pH and temperature.
This equation was developed after extensive work with
sewage systems and is shown as follows:
As
depicted in Figure 4, (Thistlewayte) this calculation
works well giving an early indication of potential for
odours detectable by neighbours. When the odour potential
rises above 30, odour complaints have been received,
as indicated by the arrows.
Figure 4: Aeration Feed Tank
Maximum Odour Potential

The
calculation method was too cumbersome, so a much simpler
method was developed using the new operational parameters.
The new calculation takes into account retention time
and is (Retention Time x Temp x Sulphide) pH. The theory
is that increasing retention time, temperature and sulphide
can cause detectable odour, whereas a higher pH will
reduce the risk. Once a calculation was formulated and
operators were confident it was "useable",
it was checked against the Thistlewayte calculation
to make sure it was not drifting to far away from the
previous work.
The
next step was a trouble shooting guide that when the
new operational odour potential result reached above
200, could be used to make sure all is in place to control
odour being detected . The following is the standard
trouble shooting checklist that is followed when a high
result or odour is detected by either external or internal
complaints.
Table
1: Troubleshooting Guide for the WWTP

Figure
5: Odour Monitoring Sheet

4.0 THE CHECKLIST
The
next step was to make this odour trouble shooting checklist
a live document that was accessible online at all times,
instead of just when problems arose. By using the Mills
online statistical data recording system known as MOP's,
an operational sheet that collected all the parameters
that we had previously identified was designed and put
online. As can be seen by the online sheet depicted
in Figure 5, it covers all sulfide results, retention
times, pH and underflow cons %. When any result is out
of its preset limit, it will alarm in red. This alerts
the operator to possible odour problems that need attention.
It also has the odour potential figure with a alarm
limit. This way the operator can check the alarm against
the odour figure to see if action is needed urgently
or monitoring will need to be followed closely until
the alarm is disabled.
Figure
5: Depiction of MOP's Alarm Screen

5.0
HAS IT WORKED?
The
Mill has enjoyed several years without a complaint from
its neighbors and we thought that could well be attributed
to the success of the odour potential figure. This was
eventually tested when starting in February, after the
mills process made changes to its dumping strategies
causing the influent flows to per average day to increase
and the WWTP process suffered causing the through-put
to be reduced. This then resulted in the AFT level rising
above its normal operating limits with the retention
time going from 24 to 30 hrs to over 80 hours. This
then related to the odour potential figure which was
now well above 500, 300 units higher than the alarm
limit. As you can see in Figure 4, within two weeks
of this plant condition we started to receive odour
complaints from our neighbors.
After
getting the plant on track and reducing the influent
flows the odour potential figure dropped below 200 and
immediately complaints ceased. This gave an excellent
indication that the online checklist was a very useful
tool. This helps us now be able to predict when odour
will become a problem for our neighbors and let us either
correct the action before it becomes an odour complaint.
6.0
CONCLUSION
Several
years of continual work on the odour problem at the
Albury Mill have paid off with a total reduction if
not removal of odour at the mill. It is only when we
experience problems outside of the plants performance
parameters that we see odour becoming a problem with
our neighbours. In conclusion it would seem logical
to work around these problems before they turn into
issues, and this is successfully being accomplished
by using the odour potential graphs and new plant parameters.
Trials
using several odour reduction chemicals such as peroxide,
biocide pellets and ferric chloride which give us a
back up in times of plant problems have been used. One
other area recently being worked with is measuring acid
producing bacteria which not only cause odour related
issues, but if present, have been identified as one
of the possible causes of filamentous bacteria in our
Activated Sludge system. It is hoped that measurement
of this bacteria in the separate production streams
may lead to reducing the bacteria and lead us to answering
problems with future odour issues and plant performance.
So,
as always with a water treatment plant, one problem
solved only gives us time to solve the next issue.
7.0
REFERENCES
Eckenfelder,
W.W., Industrial Water Pollution Control, McGraw
Hill, Singapore, 1989.
Thistlethwayte,
D.K.B., The Control of Sulfide in Sewerage Systems,
Butterworths, Sydney, 1972.
Ferris,
B, Final Report on the Pollution Reduction Program,
Norske Skog, 2000 DOWNLOAD
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