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Conference Papers | 2003 Conference Papers
USE
OF A STREAMING CURRENT DETECTOR AT WARRAGUL WATER TREATMENT
PLANT
Len
Ablett, Water
Treatment Operator, Gippsland
Water
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ABSTRACT
Warragul
Water Treatment Plant is located approximately 110 kilometers
west of Melbourne. The raw water is supplied from Pederson
Weir, with very high turbidity and colour entering the
plant during dirty water events. Gippsland Water decided
to build a new DAFF Plant, which replaced the old clarification
plant. The design of the plant included provision for
a Milton Roy SC 5200 Streaming Current Detector (SCD),
this was the first SCD to be installed and trialed at
any of Gippsland Water's treatment plants.
The
operation of this SCD required several changes to the
set-up at the Warragul site. These changes included
changing the planned Alum and pre-lime dosing points,
installing a new sample point for the SCD unit, installing
a smaller Alum dosing pump, and altering the pre-lime
dosing system to provide better coagulation pH control.
These
changes allowed the SCD to provide close control of
the coagulation at the Warragul site, including managing
dirty water events with turbidities up to 300 NTU's
and colour of up to 300 PtCo. During these events the
SCD manages coagulation dosing to produce suitable output
quality.
These
changes have significantly reduced chemical consumption
and operator input, particularly during these dirty
water events. This time is utilized for routine maintenance
and further performance testing around the water treatment
plant to better manage water quality,
KEYWORDS
Streaming
Current Detector (SCD), water treatment, turbidity,
colour, pH control.
1.0
INTRODUCTION
The
Warragul Water Treatment Plant is situated 5km north
of Warragul on the main Neerim road. It supplies water
to the townships of Drouin, Buln Buln, Rokeby, Nilma,
Darnum and Warragul. This equates to a population of
approximately 20,000 people.
The
raw water is supplied from Pederson weir on the Tarago
River which is located 8 km up stream from the Tarago
Reservoir. The raw water is supplied by gravity to the
Water Treatment Plant via a 450mm mild steel concrete
lined main, 32 km's in length with an 80 meter static
head . The supply main is limited to only 12 ML/day
to the water treatment plant due to the size of the
main and volume available from the catchment area.
The
incoming raw water turbidity varies from 5 NTU TO 400
NTU and the colour from 10 PtCo to 300 PtCo. The raw
water quality changes very dramatically, during heavy
rains and storms. Due to this variability the original
water treatment plant had a lot of difficulty, ensuring
the correct Alum feed dose and removing the colour.
Under normal operation jar tests had to be carried out
at least twice a day and more often during varying raw
water events. The water treatment was able to handle
low turbidity raw water, but did not automatically adjust
the chemical dosing during varying or high turbidity
raw water events. These changing conditions also caused
problems controlling coagulation pH.
Typical
treated water quality results from the original water
treatment plant were around 0.7 NTU to 1.2 NTU, colour
units were from 5 to 10 PtCo. During high rainfall or
storm events, significantly worse results were regularly
obtained.
Gippsland
Water was going through a process of improving, designing
and reconstruction of Water Treatment Plants. At several
sites, including Warragul, the existing plants were
very old and the technology out of date. At Warragul,
a tendering process for a design and construction contract
was commenced. From analysis of the submissions, it
was decided to construct a Dissolved Air Floatation/Filtration
water treatment plant. This was to be the first water
treatment plant of this type in Gippsland Water.
A
contract was awarded to Aqua-Clear Technology P/L from
Geelong, at a cost of $3.2M. This plant was designed
to produce 20 ML/day, and be fully automated to reduce
the operators work load and hours. Much of the design
was based on similar works undertaken by the contractor
for other authorities. During commissioning many of
the differences at Warragul were highlighted and these
had to be remedied.
2.0
CHEMICAL DOSING
The
new water treatment plant design provided for the alum
dosing point to be located 50 meters up stream from
the inlet chamber. Also the alum dose rate was manually
determined by doing jar tests. During early operation
it was determined that the pin-flocc was breaking up
in the inlet pipe, before it reached the inlet chamber.
After testing alternative alum dosing points, it was
found that 8 meters from the inlet chamber was the best
spot. This change improved the coagulation, but did
not assist control the correct dose rate, particularly
in different raw water quality. Jar tests still had
to be performed at least twice a day.
After
much consideration it was decided to develop a coagulant
dosing table (alum dose [ppm] versus raw water turbidity
[NTU]). This table worked quiet well, however because
of the indifferent raw water quality, it was not always
correct and still required many jar tests to determine
the correct dose rate and adjustment of the table. The
water treatment plant utilises a pre-lime dosing system
to control coagulation pH. This pre-lime system also
worked manually and would always under dose or over
dose, causing poor coagulation pH control, which resulted
in bad coagulation (NO PIN-FLOC).
The
original design of the water treatment plant included
provision of a Streaming Current Detector (SCD) to be
tested for suitability for controlling alum dosing in
a water treatment plant of this type. These units had
never been previously used in Gippsland Water's water
treatment plants for coagulant dosing control.
3.0
STREAMING CURRENT DETECTOR (SCD)
A
Milton Roy SC 5200 Streaming Current Detector was installed
(with no weather protection), just above the inlet chamber.
It was originally set-up with the sample being drawn
from the pressure inlet main two meters after the alum
dosing point. This model SCD unit has its own PID Controller
to control the output to a dosing pump. However it was
decided to utilize the control capabilities of the water
treatment plant PLC for this purpose.
During
every PLC program cycle the PID Control Loop the required
Alum Dose-rate Set-point [ppm] is calculated.
The
SCD output value is compared to the SCD controller Set-point,
as follows:
Every minute the PLC performs the following calculations
-
- If
the SCD output is greater than the SCD controller
set-point high limit then decrease the Alum dose-rate
set-point by one;
- If
the SCD output value is less than the SCD controller
set-point low limit then increase the Alum dose-rate
set-point by one
Where
the SCD controller set-point high limit and the SCD
controller set-point low limit are 0.5 above and 0.5
below the SCD controller set-point which is set by the
operator. Any values within these limits will not change
the current Alum dose-rate set-point. One unit SCD change
is equivalent to 0.1mg/L change in the Alum dose-rate
set-point.
The
required alum dose is then calculated by multiplying
the Alum dose-rate set-point by the raw water inflow
to obtain the dose-rate in litres/hour. If selected
by the operator, the supernatant return flow is added
to the raw water inflow for this calculation.
The
SCD unit output works with the setting and adjustment
of the gain and the zero setting. The more gain means
the higher the rate of change in the Alum dose rate
when compared to SCD value, the less gain would drop
the rate of change in the Alum dose rate when compared
to SCD value. The zero setting also adjusts the Alum
dose rate, if the zero is set on 1.00, you would automatically
lift the alum dose rate, if the zero was on -1.00 it
would drop the alum dose rate.
To
setup the SCD output adjust the Zero to "0.00",
select an appropriate control set-point (relating to
good coagulation performance) and adjust the gain(+)
to achieve the required rate of change in the Alum dose
rate corresponding to the variation in raw water quality.
This process sounds very straight forward, but this
step actually took 12 months for the SCD to be set correctly.
There are not a lot of problems in setting up an SCD,
however it takes time. Following a change to the gain,
a week of different types of water quality and jar tests
to cross check, was required to assess how satisfactory
the change was.
This
SCD unit also has its own wash cycle, with over 8 different
time settings, to wash the sensor probe to prevent contamination
of the output. The unit at Warragul is set at half hour
intervals to wash for 30 seconds.
4.0
PROBLEMS ENCOUNTED
4.1
Pre-Lime Dosing
The
next problem was the coagulation pH control and the
pre lime system, was being dosed directly into the inlet
chamber and did not get enough time to mix and react
the lime particles properly. These particles passed
though the SCD causing incorrect readings and output,
Alum over dosing and poor coagulation.
This
prompted a week of tests to find the correct point for
the pre lime, to be dosed. The best result was found
50 m upstream from the inlet chamber (prior to Alum
dosing). Another problem was that the lime concentration
strength was far too thick and was not mixed properly.
When
a dirty water event occurred it would cause a high concentration
of lime in the slurry bin with poor mixing and a lot
of lime particles would continue to pass though the
SCD causing false readings and again over dosing with
Alum, which resulted in more lime.
After
a lot of thought it was decided to alter the calculations
in the PLC regarding control of the Lime feeders, and
fit VSD's to the lime dosing mono pumps as part of a
coagulation pH control. By adjusting the speed of the
dosing pump to achieve the required coagulation pH,
better control was achieved.
In
addition, the PLC the lime feeder control was altered
to provide lime solution strength of 1% up to 50 NTU,
2% from 50 NTU to 100 NTU and 3% from 100 NTU to150
NTU. This enabled the VSD on the mono pumps to ramp
up to their maximum speeds before changing the lime
solution strength, and drop to their minimum speeds
when required to dilute the lime strength.
Now
that the dosing points for the Alum and the pre-lime
were working correctly, it enabled a trial of the SCD
control with the indifferent types of dirty water that
entered the Warragul Water Treatment plant, to commence.
4.2
Suitable SCD Sample and Installation
As
previously discussed, the alum dosing point was moved
to 8 meters from the inlet chamber, on the inlet manifold.
A submersible sample pump was installed in the middle
of the inlet chamber to provide a reliable well mixed
sample water to the coagulation pH control probe and
the SCD for more accurate response. Another reason for
choosing this location is that it was after the addition
of supernatant return water and the control system could
adjust automatically for any changes in this quality.
A
flow meter was installed on this sample pipe, so if
the pump faults, and stops pumping water to the pH probe
or the SCD unit, the water treatment plant will shut
down, and alarm out and let the operator know there
is a fault. This assists to stop any dirty (incorrectly
dosed) water entering the plant. A weather proof stainless
steel cabinet was fitted over the SCD to protect it
and ensure reliable long-term operation.
4.3
Alum Pumping System
Another
problem was the limited range the two Alum pumps had
to ramp up and down. The pumps, as provided were ranged
for 35 to140 litres/hour, to allow for the high turbidity
water that enters the water treatment plant. The two
pumps are on a duty/standy arrangement, which will automatically
swap over if one fails. With this equipment, it was
impossible to set the stroke and pulse rate for both
high and low turbidity waters. It was decided to alter
one of the pumps, and fit a 12 -35 litres/hour pump.
Then by altering the PLC program, so the low pump controlled
the low turbidity waters, then swap over to the larger
pump when required by either high turbidity or high
colour.
4.4
Highly Coloured Raw Water
At
Warragul, the raw water has high colour that enters
the water treatment plant after a dirty water event
has started to subside. The old water treatment plant
could not control this increased coloured water. The
new water treatment plant, when running on the manual
system also failed to control the colour.
The
SCD certainly proved it could control the coagulation
dosing to remove the colour from the water. The SCD
picks up the colour in the water, and ramps up the Alum
dosage by up to 20 ppm to assist remove the colour.
5.0
PERFORMANCE RESULTS
5.1
Dirty Water Events
Three
years a go when the decision was made to use the SCD,
many individuals were very skeptical about leaving a
water treatment plant with the coagulation being controlled
by an instrument and particularly since this instrument
had not been used, not only in Gippsland Water, but
at many other Water Authorities previously. It took
a while to become familiar with the unit, just to get
the zero set and determine an appropriate set-point
that was wanted. Altering the gain up and down certainly
made big differences in the coagulation of the water.
At
first, The SCD unit could control at very low Alum dosages
at low turbidity, but it would fall behind when higher
turbidity entered the water treatment plant. By turning
the gain up a tweak certainly helped the SCD control
dirty water events. It increased our Alum dose rate
marginally, and controlled the coagulation really well.
The SCD now controls the coagulation reliably under
very varying raw water conditions without any jar tests
being performed for over three years. The SCD unit has
never failed, some dirty water events, with varied turbidity
from 5 NTU to100 NTU in less than 10 minutes, with colour
of up to 300 Pt Co. These high turbidity and high colour
events occur regularly at the Warragul Water Treatment
Plant, particularly in autumn.
5.2
Colour
The
Warragul Water Treatment Plant had never been able to
reliably remove colour from the incoming raw water.
The old water treatment plant had a clarifier with no
filters, jar tests had to be performed at least twice
a day, as the PLC could not control the proper Alum
dose rate for colour removal. The new water treatment
plant, a Dissolved Air Floatation/Filtration system,
was expected to remove approximately 80% of the colour.
With
the SCD detector now working well with the turbidity
variation, the next step was to trial the SCD to see
if it could assist with the removal of colour from the
raw water entering the plant. The SCD was now controlling
the huge changes in the raw water turbidity very well,
but continued to only removed about 75% of the colour.
Although this was a big improvement, it was felt that
with more tuning of the SCD it could remove nearly all
the colour.
By
altering the SCD gain over a period of six months, the
SCD successfully managed to control the Alum dose rate
to remove the colour . Now when the high coloured water
enters the plant, the SCD automatically adjust the alum
dose-rate set-point (up to 20 ppm higher) to remove
the colour, even when the raw water turbidity is dropping
off. The colour of treated water leaving is less than
one PtCo, even during dirty water events.
5.3
Reduced Chemical Use
At
the start of the commissioning at the Warragul Water
Treatment Plant chemical consumption was very high.
Because of the manual control, more alum was dosed than
was needed because of inconsistent raw water turbidity
entering the plant.
Even
doing jar tests prompted the selection of dose rate
that produced the best heaviest flocc. This flocc was
much heavier than needed. This overdosing was to be
improved by controlling coagulation with a dosing table
(Alum dose rate verses raw water turbidity).
The
raw water from Pederson Weir is very inconsistent and
the control did not work all the time, often over dosing
the alum, causing the pre lime to also over dose. With
the SCD working correctly it lowered the dosage of alum
and lime dramatically which adjusted the coagulation
and flocc formation and definitely helped the Dissolved
Air Floatation plant. With the coagulation of any water,
you need the correct amount of Aluminium Ions to balance
the negative charges on the dirt particles. It is then
necessary to get the right flocculant dosing (polymer)
to form the size the flocc required. DAFF flocc needs
to by light and fluffy to lift easier. The SCD reduced
the alum dosage by up to 50%. Typically the lower alum
dose rate meant that the pre lime dose rate was also
dropped by 50 %. A cationic polymer (1190) was installed
at the water treatment plant to assist in removing the
colour, since the SCD detector was working to its specification,
this has not been used, even during dirty water events.
6.0
CONCLUSION
The
SCD unit controlling coagulation has made the Warragul
Water Treatment Plant a very reliable water treatment
plant, even with each dirty water event. The high turbidity
and colour prove to be no problem for the SCD. Chemical
usage of Alum and Lime has dropped by approximately
50% and the 1190 polymer is not needed at all. This
is a huge saving compared to the old plant, and the
new plant before the SCD was put on line. The operators
testing load to keep the water treatment plant performing
well has decreased by up to 60 %,(as we have not done
a jar test for over 3 years). This gives the operator
time do other water parameter tests and routines. The
maintenance of the SCD unit involves cleaning only every
three months, and takes a half an hour.
7.0
ACKNOWLEGEMENT
Thanks
to Ian Soutar, for his knowledge and support during
the setting up, testing and commissioning of the SCD
unit.
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