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Conference Papers | 2003 Conference Papers
UPGRADING
JET RODDING AT ACTEWAGL
Graeme Whelan, Plant
Coordinator, ActewAGL
Paul Wheatley, Field
Services Manager,
ActewAGL
Peter Burgess, Engineer,
ActewAGL
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ABSTRACT
ActewAGL
have four specialist choke trucks incorporating a Jet
Rodder as their primary method of cleaning sewer mains
in the Australian Capital Territory largely replacing
hand and machine sewer rods. This followed a history
of accidents with sewer rods, rodding machines and sewer
eels
Two
lost time accidents and numerous near misses using the
jet rodders prompted ActewAGL to look for engineering
solutions and training in their use.
However
it became obvious that there were underlying issues
with the jet rodders that led to a complete review of
the whole process with the following conclusions:
- Training
was ad hoc and full of misconceptions about the jet
rodder use.
- No
standard work method for cleaning sewer mains
- Cleaning
was unsatisfactory with significant revisits
- Equipment
was not treated with respect required
- Trucks
and equipment in poor condition with safety systems
bypassed.
- Problems
maintaining competence
ActewAGL
undertook a complete program, which included fixing
equipment reviewing work methods and developing training
to the new Water Industry Package Unit 255A
The
program is getting results with the machinery working
properly, reduced rework and a greater feeling of ownership
among the operators.
KEY
WORDS
Jet
rodder, sewer, training, cleaning, ActewAGL, safety.
1.0
INTRODUCTION
ActewAGL
is a private company that has ACT Electricity and Water
(ACTEW) Corporation and AGL as its shareholders. The
water division of ActewAGL carries out the water and
sewer system maintenance and operation on contract for
ACTEW Corporation. The system consists of 2,900 kilometres
of sewer mains to service some 300,000 people in the
ACT. Because of the dry climate and amount of trees
in the bush capital there are a high number of chokages
because of tree roots. Each year ActewAGL clears over
5,000 chokes 95% of these within the 5 hour customer
service response requirement.
About
5 years ago the organisation determined that the choke
clearing operation could be carried out more effectively
by using high pressure water cleaners instead of the
sewer rods and mechanised system. Part of this decision
was the amount of incidents and injuries resulting from
the use of those methods. The cold winters in Canberra
also caused problem for mechanical methods of sewer
cleaning.
ActewAGL
presently leases a fleet of 5 Jet Rodders.
Four of the trucks are set up as choke trucks and are
used on a shift rotation basis. The other truck has
a high volume set up and is used in conjunction with
CCTV for more specialised work. ActewAGL also uses the
services of a jetter/eductor contractor for stormwater
and other specialist work.
Figure
1: Typical choke truck

Following
two accidents with the jet rodders where the nozzle
left the sewer and struck a worker a safety audit was
carried out. The initial response was to look at a physical
barrier to the nozzle leaving the access chamber and
grills to cover open access chamber were manufactured
for field trials.
During
the investigation grills the Engineer Peter Burgess
talked with the operators of the machinery to find out
how the jet rodding operation was carried out so the
design could be tested. The message from the operators
was fairly clear. They thought the machines were "useless"
and didn't do the job so they wanted bigger machines.
This sentiment was echoed in the supervisor level.
Inspections
indicated the machines weren't in good condition and
weren't being used correctly. The effectiveness of the
jet rodding was well down from when they were first
introduced. In some cases the nozzle were apparently
only travelling 50 metres before stopping because the
friction of the hose. The effectiveness was well down
of the manufacturers specifications and there was no
apparent reason for the problem. Advice from suppliers
also seemed to blame the adequacy of the trucks to do
the job.
The
results of these preliminary investigations were reported
to the Field Services Manager, Paul Wheatley with a
strong recommendation that the total process be investigated
to discover the real problems as the grill was seen
as a further imposition on the field staff. This wider
investigation was commissioned and commenced in July
2002.
The
investigation was carried out with four objectives:
- Determine
why the jet rodders weren't working properly;
- Find
out what was wrong with the trucks;
- Review
the instructions and work processes;
- Review
the training and competencies.
Graeme
Whelan, the plant coordinator, was set the task of investigating
the trucks and jet rodding machines. Also helping were
the safety officer and a trainer.
2.0
INVESTIGATING THE EFFECTIVENESS OF THE JET RODDERS
A
review of the specification was carried out and this
indicated that the Jet Rodders were suitable for what
they were doing. They were in fact a very reliable unit
which should have had no trouble in giving years of
long service. The pump motor was a very reliable diesel
unit and not expected to give trouble as they were only
doing 1200 hrs per year. The pump was fairly robust
and not seen as a source of trouble.
The
trucks were set differently for example the pulley's
and drive ratios were different. However, this didn't
seem to be the major problem. Static pressure tests
where the nozzle was inserted in a stormwater in the
yard was used to test the set-up. These showed different
results for the trucks. The pressure shown was 1800
psi when the manufacturer recommended 2,000 psi. The
pressure gauge was checked and calibrated and was found
to be working properly.
The
tests pointed to the pressure relief valve as the problem.
The system uses a pressure relief system that returns
the excess pressure to the tank. The pressure relief
valves were not working properly and releasing too much
pressure and because they were inline were causing a
high pressure loss.
A
new system of operation was devised where the pressure
blow off was moved out of the main feeder line. The
pressure for relief was adjusted to 2,200 psi to minimise
the amount of bypass
A
simple test was devised to check the pressure and flow
for the trucks. This involved holding the hose without
the nozzle parallel to the ground and measuring the
distance that jet travelled. From this information the
flow and pressure available from the pump was calculated.
This indicated that pumps were working correctly and
any differences due to different hose lengths. The hoses
where replaced to the correct length of 140 metres and
a leader hose attached. Each truck was now about the
same pressure and flow.
The
in pipe tests were now repeated using the same nozzle
for the different trucks and different nozzles for the
same truck. These tests indicated that different nozzles
were the problem and were too small or too large. It
was suspected that they had been set up for the trucks
when they were not operating properly and thus were
now wrong
The
basic nozzles used for jet rodding have two actions.
Forward or sideway jets cut into the obstruction and
the rear facing jets provide thrust. The effectiveness
of the jet rodder is very dependant on the pressure
and flow at the nozzle. If the jets are too big there
will be high flow but little force and vice versa.
Figure
2: Typical nozzles
Tom
Williams from DCS industries was called in to calibrate
the existing nozzles and to fix up root cutters. All
nozzles now became interchangeable between the trucks
and thus we could reduce the inventory. Tom also pointed
out a few other problems and issues with the pumping
controls and trucks. All of these problems happened
within the next three months as predicted.
The
jet rodder were now up to scratch and field reports
started to come in indicating they were working including
root cutters. To quote an operator "I don't mind
working on these now because it does the job"
3.0
INVESTIGATING THE TRUCKS
Close
inspection of the trucks and equipment was carried out
with the following results:
3.1
Water Tanks
Close
inspection of the tank mountings revealed wear had loosened
the mounting straps and they could be pulled out of
position.
The
tanks had been supplied unlined and were starting to
leak. These have been sealed. Internally the baffles
were broken and made the tanker unstable when full.
These were reinstalled.
3.2
Location of Valves and Pipework
The
pressure lines and valves were set up on the truck during
assembly. The last item assembled was the tank so that
many of the working parts and valves were under the
tank and not accessible or maintained. The "pressure
on" valve could not be opened more than a quarter
turn. On some trucks there were seven small diameter
connectors located on a straight pipe under the tank.
All these factors contributed to poor performance of
the machine.
The
pipework was replaced in larger 25 mm diameter hose
and connectors. For some of the trucks replacement pipes
were threaded through and replaced with operating valves
relocated to where they were accessible but covered
to prevent damage. One truck had to have the tank taken
off to replace a failed main operating valve. This valve
was relocated to the outside where it was more accessible.
3.3
Operating Valve
On
one truck the linkages that connected the "pressure
on" valve and the bypass shut off had been replaced
upside down and the "pressure on" valve could
only be opened a quarter turn. This set-up was replaced
3.4
Pressure Relief Valve
These
were broken or not set up properly. The principle of
these jet rodders was that when the pump pressure reached
2,000 psi the pressure relief valve would start to open
and relive the pressure. This was a safety device to
protect the pumps. However as the Jet Rodders are supposed
to work at 2,000 psi this set up is marginal and the
pressure relief valve would be constantly operating.
In
our case the pressure setting was below 2,000 and the
valves were wearing out through constant use. As they
were online it was found that we were losing some 400
psi in head losses. A decision was taken to increase
the relief pressure to 2,200 psi to minimise the working
of the relief valve.
A
different set up was also manufactured where the relief
valve was placed off line. To operate the pump the bypass
valve had to be shut and this was fail safe to open
position. This set up is under trial.
3.5
Hose Reel Hydraulic System
The
hydraulics for winding the reel in and out were not
very effective. The operators were pulling the hose
back by hand. It is suspected that the oil filter in
the hydraulic lines had never been changed as it was
in a rear cabinet and not on the engine maintenance
schedule. The hydraulics were serviced and are working
to full capacity.
3.6
Road Worthiness
Various
safety and operating features on the trucks were outside
of Australian design rules and were replaced.
3.7
Other Improvements
- An
oil bath was incorporated in the tray to take the
root cutters.
- Steps
were included so the controls could be accessed more
easily especially for the shorter operators.
- A
remote control line was included so the jet rodder
could be operated from the ground near to the access
chamber.
- An
extended hose guide was added so the hose could be
directly lowered into an access chamber
- The
trucks were cleaned professionally
- Boxes
for instructions and paperwork were installed
- Instructions
and labels were fixed near the controls
3.8
Results
The
trucks had some teething problems while this process
was carried out and sometimes only one or two trucks
were on the road. This caused a lot of truck swapping
and some grumbling but persistence paid off because
eventually all the trucks were brought up to good working
condition. The other advantage was that the operators
were able to try out different trucks and were able
to comment on any differences they found.
All
operators have a check sheet for the trucks and nearly
all faults are being reported, and are fixed. This has
helped the operators to understand the jet rodders and
to look after the trucks and is a big part of the change
in work practices. This system is not perfect because
of the high changeover of personnel through the trucks
but it is much improved and the trucks are in better
condition.
4.0
REVIEWING THE INSTRUCTIONS AND WORK PROCESSES
The
instructions had not been updated for some time, they
were very basic and based on a type of truck that no
longer existed. The instructions did not address the
whole system of work and did not indicate a standard
method.
Interviews
with experienced operators indicated many misconceptions
and different work practices were being passed on from
team to team.
One
misconception was that the jet rodder had to travel
at high speed to punch a hole in the choke whereas the
proper procedure is to let the water jets do the work.
Contact with the choke is counter productive and allowing
the nozzle to fly freely is hazardous. Teams were manually
retracting the hoses risking injuries. The teams were
clearing the water back up rather than fixing the choke
and this was leading to further blockages at the same
point
An
overall review of the system blockages was carried out
and it was that the teams were returning to the same
site twice and sometimes up to six times (See figure
3). It was determined by the field service manager that
we should look at the work practices and try to reduce
this figure as based on a cost of $165 per choke and
some 680 revisits a saving of up to $112,000 per annum
was possible.
Figure
3: Number of multiple visits to properties

The
main issue here was the difference between unblocking
the pipe and removing the blockage. It is possible to
punch a hole through the choke and to release the water
backed up but this self seals and within two days the
choke is back. Where there is some clearing of the roots
the choke can take a bit more time to come back but
this can be as short as three months.
It
was decided that the work practice would change so that
the crews removed the blockage so it would remain free
for a longer period. The work method became to use a
jetting nozzle to pierce the choke and then use a root
cutter to remove the choke. This method was included
in the training package and was to become the standard
method. This became possible because when the choke
trucks were brought up to specification they could easily
run the root cutter.
This
change in work practice has been incorporated in instructions
and training. It is too early yet to gauge the results
but the feedback from the field indicates that the amount
of rework has reduced and the change in work practises
5.0
TRAINING AND COMPETENCY
Training
had been carried out but this was purely about the operation
of the pump and motor not about the cleaning method.
With the release of the new national training package
this training course was seen as a first step to gaining
national qualifications for the operators. ActewAGL
is a registered training Organisation and is able to
issue certificates. The training package was organised
so that it would met the requirements of the competency
unit NUW 255A Maintenance of Sewer Systems.
The
training was carried out in two phases. Classroom style
training was carried out for one day and on the second
day the operators were taken to a purpose built training
area at Mitchell depot for initial induction and competency
assessment. Further assessment is planned in the work
location so the operators can gain their certificate
of attainment.
The
training package is flexible and can be adapted to the
different skill levels of the operators. All of the
sessions were fairly lively with a lot of input from
the operators. A lot of this discussion was about how
to make the system work better now that the equipment
was working well.
6.0
SAFETY
Safety
was one of the key drivers for this investigation and
change. The accidents were happening to more experienced
personnel rather than inexperience starter so the whole
work practice had to be examined.
Some
of the more important aspects of safety was a lack of
understanding or willingness to comprehend the power
of the high pressure water and the force that the nozzle
could exert. The other problem was the bacteria in the
sewer that could be forced below the skin and create
extreme problems for recovery if not informed. All operators
now carry a health warning card.
Most
of the other safety problems had to do with the inadequacy
of the machine. Pulling the hose by hand etc was all
a result of the poor state of the equipment. Even simple
items like a work light were installed as part of the
review.
The
safety has improved and no further accidents directly
applicable to the jet rodders have been reported. However
regular checking will be carried out to ensure this
high standard remains.
7.0
SUMMARY OF THE FINDINGS OF THE INVESTIGATIONS
The
whole of the jet rodder operation was found to be flawed
and inefficient.
- Ad
hoc training passed on from one employee to another
full of misconceptions about the jet rodder use.
- No
standard method
- Poor
results with significant rework
- Equipment
not treated with respect and poorly maintained
- Trucks
and equipment in poor condition with safety systems
bypassed.
- Problems
maintaining competence
The
result of all of the above was poor effectiveness and
increasing probability of safety being compromised as
the operators made do.
8.0
RECOMMENDATIONS
A
program that addressed all the issues at once was recommended.
It was pointless training the people if they went back
to the same old equipment that wasn't doing the job.
Training
A training course to be developed for all people involved
in Jet Rodding.
The training to be equivalent to the National Water
Industry training package - NWP 255A.
All current field staff are to undertake the training
and assessment.
A proper induction is to be carried out for all new
starters.
A specialist training area has been set up and is available
for further training as necessary.
Equipment
A major decision was to ensure the jet rodder were maintained
and in good working condition otherwise the training
would be lost. All the trucks were to be standardised
and regular checks made of their performance. A specialist
contractor is used to maintain specialist nozzles and
root cutters. An adequate inventory of spares is to
be maintained.
Trucks
Ongoing maintenance to be carried out and checklists
completed regularly to ensure the trucks are maintained
in good working order.
Work
practices
The biggest time waster is rework and new work methods
are introduced so that revisits to the same site especially
within one week are minimised.
9.0
CONCLUSIONS
The
success of this project is a result of looking at the
total issue to ensure that the operators have the knowledge
skill, tools and equipment to carry out the work properly.
The enable this to happen each of the following areas
has to be addressed and checked on a regular basis.
-
Equipment
- Trucks
- Work
Method
- Training
If
these aspects are in place then the safety of the work
and operators satisfaction is improved. DOWNLOAD
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