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Conference Papers | 2001 Conference Papers PROBLEMS
ASSOCIATED WITH OZONE/GAC AS A FINAL DISINFECTION
Roland Passuello -
Water and Wastewater Treatment Operator,
NERWA
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KEY WORDS
Disinfection,
Granular activated carbon (GAC), Biological activated
carbon (BAC), Ozone, North East Region Water Authority
(NERWA)
ABSTRACT
Mt
Beauty is a small town, which uses Ozone to disinfect
water to a population of 2,700. Water quality is of
a high standard not needing treatment before entering
the Ozone Plant. The plant delivers between 1 and 3
Megalitres per day and is simple to operate requiring
minimal time. The final water has no taste and odour
problems but does appear white in colour, which creates
public concern. Backwashing problems in the GAC filters
have caused biological growth resulting in failures
to comply to WHO standards. In this paper I will cover
all the operating problems, and issues associated with
Ozone/GAC as a final disinfectant.
1.0
INTRODUCTION
Mt
Beauty, Tawonga and Tawonga South are a group of small
towns situated in the Kiewa Valley in North East Victoria.
Population is 2,700 but reaches 5,000 to 6,000 during
peak tourism times. The water supply comes from the
West Kiewa River catchment below Mt Hotham. It is collected
from the Southern Hydro Electricity tunnel and gravity
fed to an open storage which then passes under pressure
through the Ozone Plant on town demand, typically ranges
from 1-3 ML with raw water quality considered excellent
- see Table 1.
North
East Water signed a Memorandum of Understanding with
the Victorian Government to provide drinking water,
which met World Health Organisation (WHO) Standards.
The available system was not able to meet these requirements,
so a process was initiated to update the system to one
which was acceptable to both North East Water and to
the community.
North East Water began by consulting an elected group
of people from the community to choose a form of disinfection
that everyone was happy with. The use of chlorine was
immediately eliminated and Ozone or UV were the only
options considered, even though it was pointed out that
these process's did not leave a residual within the
reticulation and were at high risk of failing microbiological
quality. The township had a referendum and voted on
a choice of 3-disinfection process's:
1. Chlorine (at no cost to the consumer)
2. Ozone (at a cost to the consumer)
3. U.V (at a cost to the consumer)
Ozone
was clearly the most popular alternative for the community.
Consequently, in early 1999 construction of the Ozone/Granulated
Activated Carbon (GAC) plant commenced and construction
was completed with the plant online in late December
1999.
Ozone/GAC was something new to me as an Operator even
though North East Water were already operating an Ozone/UV
plant at Myrtleford. Mt Beauty's Ozone plant was very
different as it totally relied on ozone to complete
the disinfection, whereas Myrtleford utilised UV directly
after Ozone, thus eliminating any carry through bacteria
from the GAC filters. The Mt Beauty plant has experienced
very few problems but the main ones we have had to deal
with have been:
| » |
The
presence of Coliforms throughout the reticulation
system not meeting the W.H.O Guidelines and Zero
Coliforms at the consumers tap being very hard to
achieve. |
| » |
Problems
with air in the water that have caused some concern
with the consumers. |
| » |
Programming
problems. |
This paper will discuss the problems we have had with
the plant during commissioning and what solutions we
have employed to overcome them.
Table
1: Mt Beauty Raw water Quality

2.0 PLANT DESCRIPTION AND COSTS
2.1 Plant Description
Raw water is gravity fed into the plant from the Tawonga
storage basin (capacity 4.5ML). Ozone is produced using
the electric Corona Discharge method, which is flow
paced and uses residual trim to control the volume of
ozone injected into the mixers.
Figure
1: Schematic of the Mt Beauty Ozone Plant

Water
is delivered to the plant via two equal sized pipelines
where an onsite Programmable Logic Controller (PLC)
determines whether it should use one or two of these
lines depending on demand. It firstly passes through
the Hydrokinetic mixers where Ozone is mixed into the
water. Ozone is delivered to the mixer using a Venturi
controlled by the volume of water being pumped.
Once
the water is mixed with the Ozone it then passes through
the contact tanks where the ozone reacts with the water
to complete disinfection. Levels of Ozone residual are
measured by samplers located downstream of the contact
tanks, and a signal is sent back to the generators so
that the set limit is maintained to achieve an active
level of ozone required to guarantee a 100% kill. The
Ozone design parameters can be seen in table 2.
Table
2: Ozone plant Design Parameters

Before
entering the town's reticulation the Ozone needs to
be removed this is achieved by passing the water through
Granulated Activated Carbon (GAC) filters (using Coconut
Fibre Carbon).
Water passes through the filter bed and Ozone is removed
in the top 100 mm of carbon, after which it enters the
reticulation. A major safety feature of the PLC program
detects high Redox in the treated water. Redox Potential
is measured on water that has passed through the GAC
to ensure that all excess Ozone is being removed in
the filter. The PLC will send an alarm if Redox Potential
exceeds the set point.
When
the set point is exceeded the PLC will determine which
GAC filter is failing by sampling each line individually.
The PLC then signals the Ozone generator to shut down
and close all valves associated with that line, an alarm
is then initiated.
Any excess air that is produced during the process is
released through the degassing valves located on top
of the contact tanks and the GAC filters. Filters are
backwashed daily with Ozonated water to prevent biological
growth occurring on the filter bed. Settled backwash
wastewater is pumped back to the raw water storage to
be reused.
| 2.2
Design Features |
| » |
Fully
interactive PLC touch screen to give operators control
of critical parts of the process. |
| » |
Flow
through design is simple to understand and use. |
| » |
Process
equipment is very easy to use. |
| » |
Low
maintenance requirements. |
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Redox
meter to monitor ozone-entering reticulation. |
The plant was constructed in 1999 at a construction
cost of $520,000. All connecting pipe work and modifications
to Mt Beauty's original water supply storage cost $395,000.
2.3
Commissioning
The plant was brought on line in December 1999 to meet
the year 2000 deadline. Changes were made and preliminary
work was completed before start up. These included:
| » |
Air
scouring water mains |
| » |
Redirection
of water mains |
| » |
Changing
storage from No 2 Reservoir supply to No 1 Reservoir
(1 ML) supply. |
| » |
Covering
No 1 Reservoir (Mt Beauty supply) |
3.0 OPERATIONAL ISSUES
During
the 18 months of the Ozone plant operating, the problems
we have faced include:
1. Air in the water
2. PLC programming problems
3. Not meeting WHO Guidelines for drinking water -ie.0
Total Coliforms
4. Ozone Residual set points
5. Backwashing problems
3.1
Air in the water
Problems have occurred within the reticulation with
milky water this is caused by pressurised air in the
water presenting itself only when the water is brought
out of the pressure situation into the atmosphere. When
a glass of water is filled from the tap it is clear
at first, then micro bubbles form and slowly rise to
the surface (a mini DAF plant in a glass). There are
no ill effects caused by this problem but the residents
prefer to have water that is aesthetically normal to
look at. The degassing valves at the Ozone plant were
designed to remove all air from the process before entering
the reticulation, whilst the valves remove the majority
of the air; some still passes through to the customer.
The contractor is currently looking at the problem and
considering installing a tank to be used as a degassing
tank before entering the reticulation.
3.2
PLC programming problems
The PLC program was designed by a North East Water employee
in consultation with the contractor responsible for
constructing the Ozone plant. As the program was new
and untested, problems were expected. The initial problem
was the PLC program not completing its tasks as designed.
The worst faults appeared in the sequences involving
backwashes. All of these issues have now been corrected
and as time passes, additional changes have been made
to make the process more efficient.
3.3
Not meeting WHO Guidelines for drinking water
In the beginning it was clear that meeting the guidelines
would be very difficult with the new Ozone plant, as
there was nothing being added to leave a residual in
the reticulation. Test results were all over the place
- see Table 3, and it appeared that the only
glimmer of hope was that the system might work was if
we could correct all the problems. Testing samples taken
after Ozone contact but before the GAC filters was used
to determine whether we were achieving full disinfection.
This was crucial if we were to have any chance of meeting
the guidelines.
Testing
regularly was the only way to pinpoint the problem as
we had been relying on the monthly sampling which only
gave us a small window of what was happening. Through
the increased sampling we discovered that the critical
component to cleaning up the plate count and coliforms
lay with the backwash sequence and if we couldn't get
this right we had no chance at all of meeting the guidelines.
We also noticed that it if the backwash was performing
correctly it took approximately 6 to 8 weeks for the
coliforms to decline and sometimes disappear within
the reticulation.
Table 3: Bacteriological Testing

3.4 Ozone Residual Set Points
It was decided when the plant was commissioned that
the set point for ozone residual would be 0.3 mg/L as
this was a level that would achieve total disinfection.
Later we found that although 0.3 mg/L was sufficient
to disinfect the water it did not provide enough flexibility
when high flows were present at backwash or high demand
periods see Figure 2. Consequently the Ozone
residual decreased to the point where it was no longer
effective. An increase in the set point to 0.4 mg/L
was trialled and is the current setting.
| 3.5
Backwashing and GAC Filter Problems |
| » |
Converting
to Biological Activated Carbon Filters at low flows.
|
| » |
Loss
of Ozone during backwash. |
| » |
Backwash
flow rates too low. |
| » |
Backwash
times too short. |
| » |
Frequency
of backwashes. |
Trials
and Remedies Employed
Converting to Biological Activated Carbon Filters
at low flows:- Through a series of tests we discovered
that the plate counts were a crucial indicator for assessing
the condition of the filters and the formation of Coliforms
within the filter bed. When the Plate counts increased,
the Coliform count would increase thus indicating that
the backwash was not effective and needed correction.
Without the correct volumes of backwash flow the filters
were slowly turning into Biological Activated Carbon
filters.
Loss
of Ozone during backwash:- Once the plant performance
was monitored using the trend graphs, see Figure
2, it was apparent that at 50 l/s the Ozone generators
could not maintain the Ozone at 0.3 mg/L during backwash.
When backwash was initiated during low flows it was
discovered that one generator was in the pause mode
when backwash began causing the filters to be backwashed
with water that was low or had no ozone thus not effectively
disinfecting the filter bed.
To
correct this problem the Ozone minimum set point was
increased to 0.4mg/L and it was decided to modify and
add changes to the PLC control, at this point we entered
a program, which was time adjustable on the touch screen.
We now can make the ozone generator which was in the
pause mode come on before backwash begins. This system
will be supplemented with a software modification that
the contractors are suppling to adjust the ozone generator
to accept a 20 ma signal. This will indicate to the
generator to ramp up to full capacity during backwash
and remain there until backwash is completed. The first
stage of this program change has been operated for a
very short time and already has shown promising improvement.
Figure
2: Trend Graph - Ozone Residual During High Backwash
Flows

Backwash
flow rates too low:- With the introduction of higher
backwash rates of 50 l/s and an increase in the Ozone
set limit the filters began improving with lower Plate
counts and Coliform counts declining. Regular testing
showed plate counts still remained higher than expected
and Coliforms were lower but still present.
Backwash times too short :- Another proposal
looked at is to increase the backwash time from 180
seconds to 360 seconds. At present this would require
an upgrade of the backwash storage tank and the software
modification to maintain constant ozone residual during
backwash.
Frequency
of backwashes :- At present backwashes are done
on a daily basis but in the future we believe that with
the longer backwash times we may be able to backwash
every 2 to 6 days. In this area we have total control
through the PLC touch screen where we can backwash both
filters daily or at intervals of one to seven days.
4.0
CONCLUSION
Seeing
the changes occurring within the water industry it has
been the attitudes and the way we perceive these changes
that has resulted in North East Water upgrading its
facilities. The need to improve the treatment of the
water, safety and ensure community consensus has been
a major challenge. The Ozone plant has been and continues
to be a challenge, but working through the problems
has led to a great expansion of knowledge, which I may
never have obtained elsewhere. It has been very difficult
in obtaining assistance with our problems as this scale
of Ozone/GAC system has not previously been used as
a stand alone system to disinfect whole town supplies.
It is more commonly used in the water treatment of swimming
pools and to help reduce chemical costs in treating
potable water supplies and also to reduce the effects
of Algae toxins and taste and odour problems.
Living in the town and having to participate in the
decision making from the ground up, including discussing
with the local community the options was in itself a
big learning curve. The Ozone plant now has been operating
for 18 months with a range of problems, which we have
now been able to reduce. These problems have been identified
and rectified as we slowly understand them. The major
issue has been correctly backwashing, but as time goes
by the results have begun to improve giving us a better
insight into the process. It is not certain what the
future holds but as it stands, the Ozone Plant shows
promise and brings forward the fact that North East
Water are working in cutting edge technology, and perhaps
we will be used as an example of what can be done.
5.0
ACKNOWLEDGEMENTS
Aqua-
Tec Fluid Systems Shepparton and Prominent for construction
and design of the plant. The residents of Mt Beauty
for standing up and believing in what they wanted. All
those who assisted me with this paper.
6.0
REFERENCES
World
Health Organisation, "Guidelines for Drinking -water,
Vol.1, 1984"
"Applications
of Ozone in Water treatment Advantages and Disadvantages"
- Ortwin Leitzke, Philaqua
"Alternatives
to Chlorine for water disinfection" - Nicholas J Ashbolt
"Implementing community acceptable means of disinfecting
water supplies for small towns in North East Victoria"
M.C. Leak North East Water. > DOWNLOAD
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