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Conference Papers | 2001 Conference Papers WARRAGUL
WATER TREATMENT PLANT - COMMISSIONING AND OPTIMISATION
Len Ablett -
Warragul Water Treatment Plant Operator, Gippsland
Water
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ABSTRACT
Gippsland
Water has undertaken a review of water treatment plants
and is modifying them to improve their performance in
meeting World Health Organization quality parameters.
A number of existing plants are very old and employ
outdated technology, so where necessary, design and
construction of new water treatment plants is also being
considered and implemented.
Gippsland
Water has opted to build a number of small package plants
for communities where treated water production is less
then three megalitres per day. Water treatment plants
supplying water to larger areas including Moe, Warragul,
Traralgon, and Morwell also required major extensions
and refurbishment. In particular, the Warragul site
posed a real problem in that it consisted of a 6m by
6m tin shed containing dosing pumps, chemical storage
and instrumentation, a clarifier tank that was at least
fifty years old and no filtration.
Clearly,
modifications to the existing plant would not have been
appropriate, so the Authority decided to construct a
new plant. A Design and Construct tendering process
was undertaken and a new Dissolved Air Flotation water
treatment plant (DAF) was constructed. This is the first
plant of this type in Gippsland Water's region.
After
commissioning, the plant performance was still well
below Gippsland Water's expectations and a number of
process modifications were undertaken. This paper outlines
some of these problem and the remedial actions undertaken.
1.0 INTRODUCTION
Warragul
is located approximately 110 kilometers east of Melbourne.
The Warragul Water Treatment Plant is situated 5 km's
north of Warragul on the main Neerim South road and
supplies water to Drouin, Buln Buln, Rokeby, Nilma,
Darnun and Warragul. These towns have a combined population
of approximately 20,000 people.
The raw water is supplied from Pederson Weir, located
8 km's up stream from the Tarago Reservoir. The raw
water is supplied by gravity to the water treatment
plant via a 450 mild steel concrete lined main, 32 km's
in length and an 80m static head pressure. Hydraulic
and reservoir supply limitations mean that the gravity
main can supply only 12 ML per day.
The incoming raw water turbidity varies from 5 to 400
NTU, the Colour from 10 to 200 TCU. The raw water quality
changes frequently, particularly during heavy rains
and storms, and the old treatment plant had a lot of
difficulty removing colour. It was able to handle low
turbidity raw water, but did not automatically adjust
the chemical dosing during varying or high raw water
turbidity events.
The
old plant had problems coping with the variable raw
water quality with typical final treated water quality
results ranging from around 0.7 to 1.2 NTU and colour
ranged from 5 to 10 TCU for good quality raw water.
Results were often much worse depending on the weather
and raw water quality.
2.0 PLANT DESIGN
The
design of the new treatment plant has a total capacity
of 19 ML/day with two filter cells, each capable of
9.5 ML/day. The raw water enters the inlet mixing chamber
where pin floc is formed. It then flows over two separate
weirs into the flocculating chambers. There are then
two flocculating tanks on each cell which mix on a two
to one ratio. The first tank stirs at twice the speed
of the second and the majority of agglomeration takes
place in the second tank, where mixing speed and velocity
is slower.
The water then progresses to the DAF chamber where the
recycle water, incorporating the dissolved air, is added.
The tiny air bubbles that are entrained in the water,
float particles to the top before entering the main
filter cell. Each filter cell has the filter media at
the bottom so the treated water passes out the bottom
of the cell. The filtered water is then pH corrected
and flows via gravity to the reservoir. Each filter
cell is approximately 7 m long by 5 m wide and 2.1 m
deep.
The
filter media is 1.8 m deep and comprises of the following
layers:
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100
mm of 6 to 12 mm gravel, |
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100
mm of 6 to 3 mm gravel, |
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100
mm of 3 to 1 mm gravel, |
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300
mm of 0.8 to 0.9 mm sand |
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1200
mm of 1 to 1.1 mm filter coal (other wise known
as anthrocite). |
The
general DAF design had worked well in other areas of
the State, particularly where manual control was utilised
and where raw water was of a consistent quality. In
order to achieve the project goals including reliable
operation, high quality treated water and a minimal
operator attendance requirement, several basic changes
to the DAF plant were necessary due to varying raw water
conditions. The Warragul raw water was particularly
difficult to treat given that turbidity could vary from
10 NTU to 100 NTU in the space of two hours. Several
faults with the plant were identified and works as outlined
below were undertaken to improve the plant performance.
3.0
PROBLEMS IDENTIFIED AND IMPROVEMENTS UNDERTAKEN
3.1 Raw Water
The raw water turbidity meter was located in the laboratory,
approximately 50 m away from the sample point at the
inlet chamber. The sample line was a large diameter
dead end pipe. The turbidity meter installed is a Hach
1620 which requires a flow of only 500 ml/min. Due to
the distance from sample collection to meter and the
low flow rate, the suspended particles in the raw water
settled in the sample line prior to reaching the turbidity
meter. This meant that the sample was not representative
of the incoming raw turbidity. To overcome this problem,
the turbidity meter was relocated close to the inlet
chamber and a sample pump fitted to ensure full flow
to the turbidity meter at all times. This corrected
the problem and the plant raw water readings changed
in line with the incoming raw water.
3.2
Chemical Dosing
The original treatment plant design provided for the
alum dosing point to be located 50 m upstream from the
inlet chamber and the pre lime dosing point (for pH
correction to allow coagulation) in the inlet chamber.
It was determined that the pin floc was breaking up
before it reached the inlet chamber and the pre lime
dosing did not have adequate time to correct the pH,
to allow the reformation of pin floc in the flocculation
tanks.
The
pre lime dosing point was moved 50 m upstream from the
inlet chamber (where the alum was originally dosed),
to provide good mixing and the alum dosing point was
relocated to 10 m before the inlet chamber. These changes
worked well and provided good chemical mixing and conditions
for coagulation. This enabled the treatment plant to
operate well during consistent raw water quality, however
still requiring to manual adjustment of chemical dosing
as raw water quality changed.
3.3
Automated Alum Dose Adjustment
After much consideration, a dosing table was developed
(alum dosage versus raw water turbidity, NTU) and tested.
Although this table worked quiet well, it was proven
not completely accurate, meaning that many jar tests
were still required to determine the chemical dose rate.
The design of the DAFF plant included provision of a
Streaming Current Detector (SCD) to be tested for suitability
for controlling alum dosing in a treatment plant of
this type. These units had not been used previously
in Gippsland Water's plants for alum control. Once this
unit was installed and operating, its performance was
monitored.
After about three months of monitoring, testing and
adjustment, involving several high raw water turbidity
events, the (SCD) was able to ramp the alum dose rate
up and down depending on the incoming raw water turbidity.
The (SCD) also allowed for the colour variation and
adjusts the alum and 1190 polymer doses to the correct
levels. The (SCD) unit is susceptible to sudden pH variations
however, with the pre lime dose point being 50 m upstream
from the inlet chamber, it allowed the lime to be well
mixed so that no lime particles could cause a false
reading. This unit proved successful, not only ensuring
the correct alum dose to maintain treated water quality,
but it also optimised the alum and the lime dosages.
The typical lime dose rate under good raw water quality
reduced from 12 mg/l to 4 mg/l.
With the improvement in pre lime dosing, the pH control
loop required retuning including fitting VSD's to the
dosing pumps on the lime system. This meant that as
the alum dosage altered, the pre lime dosage adjusted
as well to maintain consistent conditions for coagulation.
Even with this system operating, the final water quality
was still not up to Gippsland Water's expectations of
<0.1 NTU, 0 TCU and <0.05 residual alum in the filtered
water.
Figure 1: View of Streaming
Current Detector and Pre-Lime pH Meter installation

3.4
Polymer Dosing
After completing modifications to the coagulation system,
the flocculant characteristics of the water was then
reviewed. After a long week of jar tests testing various
chemicals, it was determined that an additional coagulation
polymer and better application of the flocculant was
required.
After
jar test trials using numerous different polymers, two
polymers, one cationic (1190) colour stripping polymer
and LT 24, a Flocculant polymer were preferred. Initial
tests involved dosing the 1190 in separate locations,
however the best results were achieved by mixing it
with the alum, at the dosing point.
The next challenge was to change the LT 24 poly dosing
points to improve control and application. From past
experience, solenoids were not the answer as they continually
block up. A modified design involving ball floats, a
needle valve and a flow tap was installed. This enables
flow versus time tests to be performed, to equalise
the dose flow into each cell. It also enables the plant,
while doing a back wash, to lift the ball float and
cut off the poly flow to the cell being back washed,
thus ensuring correct poly dosing continued to the other
cell. This system works extremely well, never blocks
from the sticky polymers, and is totally independent
from any electrical signal.
The
water quality now exceeded expectations with the turbidities
for floated water reducing to between 0.6 and 1.0 NTU,
filtered water to 0.03 NTU and all the colour was removed.
Figure
2: View of Flocculant Dosing Point and Isolating Ball
Float

3.5
Pre-Lime Dosing
When the plant inflow reduced 50% during a back wash,
the pre-lime dosing pumps could not push the lime solution
into the increased pressure in the incoming raw water
main.
Two
lime solution water carrier pumps were fitted to the
lime dosing lines, to increase the pressure of the dosing
system. This improvement worked well for a while, but
it did not take long for these pumps and the dosing
lines to block. A high pressure water line was then
fitted to the dosing lines, with a solenoid valve set
on a timer, to routinely flush the pumps and lines at
set intervals. In addition pipework was set up to allow
the provision for a 1% hydrochloric acid wash (if required)
to clean the lime dosing lines and pumps. This later
addition is not needed as the water flushing keeps the
system clean, without any additional maintenance.
To further reduce blockages and dosing pump operation
problems, the lime solution strength was reduced. The
original lime solution was around 5% which is too concentrated
for the lime system to work with out regular maintenance.
The lime dosing pumps were also operating at very low
speeds and this caused dosing line and pump blockages.
The
lime solution mixing tank has a capacity of 200 litres
and in order to change the dosing solution to meet changes
in raw water quality, at least 20 minutes would be required
to allow change of solution strength. This caused problems
with adequate response times in line with alum dose.The
solution strength was reduced to 1% and working with
the dosing pumps speeds, an algorithm was developed
and programmed to maintain a 1% lime solution until
the raw water turbidity reached 50 NTU. At this point
the solution changed to 2% to assist with the increased
alum dose utilizing the VSD's on the lime pumps.
Larger,
higher pressure carrier pumps were fitted so that only
one pump would need to run to overcome the highest pressures
in the raw water main. When the incoming flow drops
below 8 ML per day both carrier pumps can run if required,
to overcome the higher static head pressure in the main.
This system has been in operation for 10 months with
minimal maintenance being required and with correct
control of coagulation pH occurring.
Figure 4: View of Lime Dosing
System (Mixing tanks in the back, dosing pumps in the
foreground and carrier pumps to the left)

3.6
Cell Floats
The solids raised by the DAF process were removed from
the cells every two hours. This process takes 4 minutes
with the floated solids discharged to the waste water
lagoon. During high turbidity events additional solids
are floated and the sludge blanket can become very thick.
The PLC program was altered so that when the raw water
turbidity reaches 50 NTU, the solids removal from the
cells will be undertaken every 1 hour, again for 4 minutes.
This enables the sludge blanket in each cell to be kept
stable.
3.7
Service Water
The original service water pump system was located in
the chlorine room, approx 200m away. The service was
capable of producing 600 kPa and the service water was
used in the chemical dosing system. After modifying
the lime systems, at least 700 kPa was necessary to
service all requirements.
The recycle water from the DAF system was capable of
750 kPa, therefore it was decided to try it as the supply
of the service water. A problem with this sytem was
that when the plant was shut down, the air from the
DAF system would enter the service water pipes and pressures
would build up in the pipes. It then blew an elbow off
a service water pipe due to built up pressure. It also
effected the DAF performance, particularly during dirty
water events, because water flow was being redirected
to the service line.
Following further review, it was decided to fit new
service water pumps that were capable of 1200 kPa, with
an adjustable relief valve to control the maximum pressure.
This pressure exceeded the volume required to ensure
the chemical dose systems worked correctly. This modification
also provided additional capacity should plant duplication
be required to meet future water demand.
The
service water offtake was connected to the out going
manifold from the plenum on each filter cell so that
treated water to dose chemicals would be available under
all operating scenarios. This gives the option of two
supplies (one on each filter cell), so that if it was
ever decided to only run one cell, a valve can be closed
isolating the cell that is off line. It also provides
the benefit of clean water. These pumps were set up
on a duty select system, so that if one of the pumps
failed the other pump would automatically start up.
3.8 Plant Operating Fail-Safe
Systems
Following a review of the treatment plant fail-safe
alarms, the following options were implemented to avoid
dirty water entering or leaving the treatment plant.
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SAMPLE
FLOW METER - A flow meter was installed on the pumped
sample line that supplied water to the incoming
pH meter and the streaming current detector so that
if the pump stopped the PLC would automatically
shut the treatment plant off and send an alarm to
the operator. |
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pH
ALARM - Alarm parameters were set for the incoming
pH, with low and high set points of 5.6 and 6.6
respectively. If the raw water pH moves outside
these settings, the treatment plant would automatically
shut down and send an alarm to the operator. |
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RAW
WATER QUALITY - Alarm parameters were set for treated
water leaving the treatment plant exceeding 0.5
NTU, the treatment plant automatically shuts down
and sends an alarm to the operator. |
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RAW
WATER FLOW CONTROL - To assist in controlling high
raw water turbidity events, the ability to reduce
raw water inflow based on turbidity measurements
was developed and installed. This can also be used
to shut the treatment plant down, if required for
extreme events. |
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STORAGE
START/STOP LEVELS - Level sensors were fitted the
main storage reservoir and the chlorine contact
tank to stop and start the treatment plant on water
levels. High and low level float alarms were also
fitted as a safety back up. |
3.9
Noise Room
The main plant room area housing the compressors and
air scour blowers was an open room with noise levels
exceeding specified limits. A sound proof room was constructed
and the noisy compressors, blowers and DAF recycle pumps
were relocated into this room. This relocation cut the
noise levels so much that the additional works of covering
the treated water outlet chamber (a noise not heard
before) needed to be undertaken. The treatment plant
is now very quiet, and a comfortable place to work.
3.10
Chlorine Contact Tank
A new roof was built over the old clarifier and it was
converted to a chlorine contact tank with a full capacity
of 4.2 ML. The roof was constructed from painted aluminium
to blend in with the surrounding environment, and to
provide a minimum life of 40 years.
The chlorine contact tank enables the required dose
of chlorine for primary kill, and allows a consistent
residual of around 0.3 mg/L to be maintained instead
of losing most of the residual through the day. After
leaving the tank the water is further chlorinated to
maintain a residual up to 0.6mg/L before entering the
reticulation pipe works.
This
contact tank has an added benefit in that chlorinated
water can still be supplied to customers even in the
event of a power failure.
The
main storage reservoir has a capacity of 50 megalitres.
This is to be lined and covered. This will protect the
reservoir from the spread of pathogens from birds and
animals.
3.11 Back Wash Pump Noise Proof
Room
A sound proof room was fitted over the backwash pumps
. This now means backwashing can be undertaken at any
time day or night, without disturbing the neighbours
that live adjacent to the plant.
4.0
CONCLUSION
After resolution of the above issues, the Warragul Water
Treatment Plant is now a reliable and consistently performing
treatment plant. It consistently produces high quality
water with turbidity's of 0.03 to 0.04 NTU, zero TCU
and alum residuals of 0.02 to 0.03mg/L, despite significant
variations in raw water quality.
The
additional alarming and safety features that have been
fitted protect the plant from failure, avoid dirty water
from being released into the plant, shut it down if
there is an operational fault, and prevent poorly treated
water from entering the reticulation system.
The
lime system is now low maintenance and very reliable.
A lot of work and thought has gone into this system
and it now controls the post and pre post dosing with
out fear of pump failure or blockages. The VSD's that
were fitted to the lime dosing pumps, allow the lime
dose rates to change very quickly and track the alum
dose rate to maintain the required pH for coagulation.
OH&S audits have been very positive with extra safety
features fitted to protect the operator and visitors
to the site.
5.0
ACKNOWLEGEMENT
The author wishes to thank Ian Soutar, for his experience,
knowledge and support during the alterations and works
that took place in the commissioning of the new Warragul
Water Treatment Plant. > DOWNLOAD
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